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首页> 外文期刊>Journal of Failure Analysis and Prevention >Failure Analysis of High-Pressure Compressor Blade in an Aero Gas Turbine Engine
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Failure Analysis of High-Pressure Compressor Blade in an Aero Gas Turbine Engine

机译:航空燃气轮机发动机高压压缩机叶片的故障分析

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摘要

Failure of high-pressure compressor rotor blade in an aero gas turbine engine is analyzed to determine its root cause. Forensic and metallurgical investigations are carried out on the blade and failed parts. The failure of the platform ladder is found to the first in the chain of events that led to the compressor blade failure. The mode of failure in the blade is found to be fatigue and has originated from the damaged region on the leading edge caused by dislodgement of platform ladder. The failure has caused extensive damages in high-pressure compressor module and also in downstream turbine blades as a secondary effect.
机译:分析了在航空燃气轮机发动机中的高压压缩机转子叶片的故障,以确定其根本原因。 法医和冶金研究在刀片和失败的部件上进行。 平台梯子的故障在导致压缩机叶片故障的事件链中找到第一个。 发现叶片中的故障模式是疲劳的,并且源自由平台梯子的拆分引起的前缘上的受损区域。 故障引起了高压压缩机模块的大量损坏,以及下游涡轮叶片作为二次效果。

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