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Experiences with lower furnace tube cracking in a recovery boiler

机译:回收锅炉下炉管开裂的经验

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The recovery boiler at the DMI Peace River Pulp Mill experienced severe cracking of composite tubes made of stainless steel 304L/SA210.Cracking occurred in tubes on the furnace floor,at primary air ports,at smelt spout openings,and at composite-to-composite butt welds in the lower furnace.The problem of cracking in the primary air ports was related to frequent temperature excursions in the tubes.These temperature variations were caused by the location and configuration of the tertiary air system and by the operation of the six-on-six interlaced secondary air system.Modifications made to the boiler have minimized the cracking problem.The elevation,size,and number of tertiary air ducts were changed,and the interlacing of the secondary air was reconfigured.A number of the SS304L/SA210 composite tubes were replaced with rotary-welded and co-extruded Inconel 625 and 825 tubes.
机译:DMI和平河纸浆厂的回收锅炉经历了304L / SA210不锈钢复合管的严重开裂。开裂发生在炉底,一次风口,冶炼出料口以及复合材料到复合材料的管子中下风炉的对接焊缝。一次风口破裂的问题与管内温度波动频繁有关,这些温度变化是由于三次风系统的位置和配置以及六通的操作引起的。 -六个隔行二次风系统。对锅炉进行的修改使开裂问题最小化。更改了三次风道的高度,尺寸和数量,并重新配置了二次风隔行。许多SS304L / SA210复合材料用旋转焊接和共挤Inconel 625和825管代替管。

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