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Combined Resonant Column and Cyclic Triaxial Tests for Measuring Undrained Shear Modulus Reduction of Sand with Plastic Fines

机译:共振柱和循环三轴试验相结合的方法来测量塑料细砂的不排水剪切模量

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摘要

This paper investigates the undrained shear stiffness of sand-bentonite specimens (with 0 %, 3 %, and 5 % bentonite by dry mass of the sand) prepared at the same skeleton void ratio (D_(rsk) = 35 % to 40 %) using a dry pluviation technique. The experimental program consisted of small strain tests using a resonant column apparatus and large strain tests using a cyclic triaxial apparatus. The resonant column tests were performed at three confining stress levels (50, 100, and 193 kPa) under drained and undrained conditions. A comparison of the shear modulus reduction with shear strains for both drained and undrained conditions is presented; the effects of changes in effective stresses and the rate of modulus reduction as a function of the effective stress are discussed to describe the discrepancy between the two sets of data. The results show a marginal decrease in G_(max) for specimens with bentonite, which is attributed to the presence of bentonite at the sand grain contacts. However, the presence of bentonite increases the linear elastic threshold, particularly in the case of undrained tests, in which a noticeable delay in excess pore pressure generation was measured. The strain level required in order to initiate excess pore pressure generation increased with increasing bentonite content. A similar trend was noted in cyclic triaxial tests, in which, for a given strain, specimens with bentonite generated lower excess pressure than sand specimens tested under similar conditions. Finally, a combined normalized G/G_(max) curve from both tests is presented for specimens with 0 %, 3 %, and 5 % bentonite at 100 kPa.
机译:本文研究了在相同骨架空隙率(D_(rsk)= 35%至40%)的条件下制备的膨润土试样的膨润度(砂干质量为0%,3%和5%)。使用干pl法实验程序包括使用共振柱设备的小应变测试和使用循环三轴设备的大应变测试。在排水和不排水条件下,在三个限制应力水平(50、100和193 kPa)下进行了共振柱测试。给出了排水和不排水条件下剪切模量降低与剪切应变的比较。为了描述两组数据之间的差异,讨论了有效应力的变化和模量降低速率与有效应力的关系。结果表明,具有膨润土的试样的G_(max)略有下降,这归因于在沙粒接触处存在膨润土。但是,膨润土的存在增加了线性弹性阈值,特别是在不排水的测试中,在该测试中,测量到过大的孔隙压力产生明显的延迟。随着膨润土含量的增加,开始产生过量孔隙压力所需的应变水平也随之增加。在循环三轴试验中注意到了类似的趋势,在这种试验中,对于给定的应变,具有膨润土的试样产生的过压低于在类似条件下进行试验的砂试样。最后,给出了在100 kPa下具有0%,3%和5%膨润土的两个测试的归一化G / G_(max)组合曲线。

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  • 来源
    《Geotechnical testing journal》 |2013年第4期|484-492|共9页
  • 作者单位

    Dept. of Civil, Architecture, and Environmental Engineering, The Univ. of Texas at Austin, Austin, TX 78712, United States of America;

    School of Civil Engineering, Purdue Univ., W. Lafayette, IN 47907,United States of America;

    School of Civil Engineering, Purdue Univ., W. Lafayette, IN 47907,United States of America;

    School of Civil Engineering, Purdue Univ., W. Lafayette, IN 47907,United States of America;

  • 收录信息 美国《科学引文索引》(SCI);美国《工程索引》(EI);
  • 原文格式 PDF
  • 正文语种 eng
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