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From Moratorium to 10 Rigs--BP in the Deepwater Gulf of Mexico 2010 to 2015

机译:从暂停到10个钻机 - 2010年墨西哥深水湾的BP到2015年

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"On the evening of April 20, 2010, a well control event allowed hydrocarbons to escape from the Macondo well onto Transocean's Deepwater Horizon, resulting in explosions and fire on the rig. Eleven people lost their lives, and 17 others were injured. The fire, which was fed by hydrocarbons from the well, continued for 36 hours until the rig sank. Hydrocarbons continued to flow from the reservoir through the wellbore and the blowout preventer (BOP) for 87 days, causing a spill of national significance."--Deepwater Horizon Accident Investigation Report. Everyone at BP deeply regrets what happened and the impact the accident has had on the communities and families involved. We remain committed to continuing to develop capabilities and practices to further enhance safety in order to help prevent this type of accident from happening again. We are also committed to sharing the lessons we learned, and the progress we have made since then with our colleagues and the public. In September of 2010, BP published the results of an internal investigation in what is known as the Bly report. Following this, BP launched 40 projects to address the 26 recommendations from this report and to rebuild trust among all of our stakeholders. Additionally, BP committed to the U.S. government to exceed regulatory standards in operating our rigs. In August of 2011, BP spud our first new well since the accident. Entering 2015, BP has 10 rigs operating in the Gulf of Mexico, more than at any time in our company's history. At first, the rigs experienced significant lost time due to equipment repairs. But that, along with formation related non-productive time, has been steadily decreasing. Since 2011, BP has successfully drilled 20 new wells and has made important technology breakthroughs on our some of our most challenging wells.
机译:“2010年4月20日晚,一个良好的控制事件允许碳氢化合物从马门底逃离澳门蒙托地的深水地平线,导致钻机上的爆炸和火灾。11人失去了生活,有17人受伤。火灾从井中的碳氢化合物喂食,持续36小时,直到钻机沉没。碳氢化合物继续通过井筒和井喷预防液(BOP)来流动87天,导致国家意义溢出。“ - 深水地平线事故调查报告。 BP的每个人都对发生的事故和涉及的家庭的影响感到遗憾。我们仍然致力于继续开发能力和做法,以进一步提高安全性,以帮助防止这种事故再次发生。我们还致力于分享我们学到的经验教训,并与我们的同事和公众一起提出的进展。 2010年9月,BP发布了内部调查的结果,称为BLY报告。在此之后,BP启动了40个项目,以解决本报告中的26个建议,并重建所有利益攸关方之间的信任。此外,BP致力于美国政府超越操作钻机的监管标准。 2011年8月,BP自违反事故以来我们的第一个新井。进入2015年,BP在墨西哥湾拥有10个钻机,而不是我们公司历史上的任何时候。起初,由于设备维修,钻机经历了显着的失去时间。但是,随着形成相关的非生产时间,一直稳步下降。自2011年以来,BP已成功钻取了20个新井,并对我们最具挑战性的井中的一些新的技术突破。

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