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Managing Shallow Water Flow During Tophole Drilling Operations in the Southern North Sea – A Case Study

机译:北海南海脱井钻井业务浅水流动 - 以案例研究为例

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With a shallow water flow-back in excess of 200 bbl/hr from the Top Chalk formation during the 171/2" section, the deviated exploration / development well "Well #4" was planned and drilled successfully with a jackup rig. The well was planned from a platform in the Southern North Sea. The primary goal for the 171/2" section was to safely drill to section TD, set casing and cement same with zero incident in a minimum amount of time while encountering shallow water flow. The key challenges for this well were: 1.Flowing Top Chalk Formation: The Top chalk formation flowed at all three previously drilled offset wells with 12.0 ppg EMW and approximately 200 bbl/hr. Several attempts to shut in the well and stop the flowing Top Chalk on the offset well "Well #1" failed. 2.Obtaining regulatory approval from authorities, and commitment and acceptance by all involved parties to drill the well under flowing conditions. 3.Hole cleaning and hole stability considerations when drilling with seawater 4.Permanently shutting off the shallow water flow with a two-stage cementation. 5.Rig uncertainty and general service market (in 2017): A new drilling contractor and drilling services not familiar with the peculiarities of operations in this area 6.Safety, communication and human factor considerations for a potentially hazardous non-routine operation. A collaborative well-planning and preparation process involving the operator drilling team, the drilling contractor and key service providers was critical to the success of the overall operation. The team worked together to ensure all requirements, risk mitigating measures, lessons learned from previous operations and offset wells, and human factor considerations were incorporated in the execution program. The well was successfully drilled to TD, evaluated, completed and flowed. The notable highlights from the top-hole drilling operation include:
机译:在171/2“部分期间,浅水返回超过200桶/小时的超过200桶/小时,偏离勘探/开发井”井#4“是用夹盖钻机成功钻探和钻井。井是计划从北海南海的平台。171/2“部分的主要目标是安全地钻到TD部分,将套管和水泥设置在遇到浅水流量的最短时间内与零事件相同。这良好的关键挑战是:1.圆形粉笔形成:顶部粉笔形成在所有三个先前钻孔的偏移孔中流动,具有12.0ppg emw和大约200 bbl / hr。几次尝试关闭井,并停止流动的顶部粉笔在偏移良好的“井#1”失败。 2.在当局的监管批准,以及所有参与缔约方的承诺和接受,在流动条件下钻井。 3.用海水钻井时井下清洁和空穴稳定性考虑因素。用两级胶结擦拭浅水流。 5.RIG不确定性和一般服务市场(2017年):新的钻井承包商和钻井服务,不熟悉该领域的行动特殊性6.安全,沟通和人为因素考虑潜在危险的非常规操作。涉及操作员钻井团队的合作良好规划和准备过程,钻探承包商和关键服务提供商对整体运营的成功至关重要。该团队共同努力,确保所有要求,风险减轻措施,从以前的运营和偏移井中吸取的教训,以及人为因素考虑因素被纳入执行计划。该井成功钻到了TD,评估,完成和流动。顶孔钻孔操作的显着亮点包括:

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