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Coiled-Tubing Gas Lift System Doubled Oil Production from Al-Wafa Field

机译:卷绕管道燃气升降系统从Al-Wafa领域加倍石油生产

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Recompleting the wells with an artificial lift system requires a large capital investment in addition to rigintervention,a capital which was not made available due to worsening security condition in Libya in theperiod between 2014 ? 2017,therefore,rig-less gas lift system via Coiled Tubing was chosen as the mostefficient,reliable and cost-effective technique to revive oil production from 12 dead wells.The results ofthis pilot project were very satisfactory.The technique involves running coiled tubing inside the production tubing of a dead oil well,the coiledtubing is then hung over an additional special tubing hanger,made specifically for this project,fixed onthe Xmas Tree.The gas is injected down continuously through a single point at the end of coiled tubingwhich is mixed with the oil in the production tubing annulus and helps lifting the liquid to the surface.Since compression system was not made available,due to cost cutting procedures implemented by MOG,the injection rate and injection pressure were supplied through a 2″ pipe connected to a gas well which hadhigh wellhead pressure.Since the wells had been dead for a couple of years,there was a high uncertainty in the design due to thelack of fresh data,therefore,N2 lifting with downhole slickline gauges and surface testing were utilized toobtain reliable and fresh data for the final design.Since,the Coiled Tubing Gas Lift System CTGL techniquewas implemented in Libya for the first time,two wells among 12 dead wells only were selected for the Pilotproject.The results of the two wells were satisfactory.Oil production from the first two wells increasedsignificantly from 0 BOPD to 4500 BOPD,which increased the overall total field oil production by 100%from 4500 BOPD to 11,000 BOPD.Since the reservoir communication is extremely high,nearby wells'production was positively impacted as well,and overall field production increased from 4500 BOPD tonearly 11000 BOPD in two months.The novelty of the technique comes from the utilization of the wellhead pressure of nearby gas wells asa source of injection pressure and injection rate which made reviving dead wells possible without investingin compression systems,seen as uneconomic for a pilot project.
机译:重新完成人工升降系统的井外需要大量资本投资,除了严格的资本,这是由于2014年之间是利比亚的利比亚安全条件恶化的资本而无法提供的资本吗?因此,选择通过盘管的钻机较低的气体升力系统作为恢复12个死井的造成石油产量的大量,可靠和经济高效的技术。这项试点项目的结果非常令人满意。技术涉及内部运行卷绕管道死油井的生产管,然后将线圈悬挂在额外的特殊管衣架上,专门针对该项目制成,固定在Xmas树上。气体通过在卷绕管末端的单个点连续注入。混合随着生产管道环中的油,有助于将液体提升到表面。由于玉米沼泽所实施的成本切割程序,不提供液体压缩系统,通过连接到A的2“管道供应喷射速率和喷射压力Hadhigh井口压力的气体良好。井已经死了几年,由于新的新数据,在那里,设计具有很高的不确定性矿石,N2用井下光滑仪表和表面测试采用了对最终设计的可靠性和新鲜数据.Since,连续的管道气体提升系统CTGL技术在利比亚实施了第一次,只选择了12个死井中的两个井。对于PilotProject。两种井的结果令人满意。从0 Bopd到4500个Bopd的前两种井中的产量增加,从4500 Bopd到11,000 Bopd.SINCE的整体总场油产量增加了100%。附近的Wells'Production也是非常高的,也是积极影响的,整体田间产量在两个月内从4500个Bopd Tonearly 11000 Bopd增加了。该技术的新颖性来自附近天然气井ASA注射源的井口压力的利用压力和注射速率在没有投资压缩系统的情况下使恢复死亡井,视为飞行员的不经济。

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