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Integrated BHA Improves ROP by 62 in ERD Operation Saving 29 Days Rig-Time, Sets Russian Lateral Length Record

机译:集成的BHA在ERD操作中提高了62%,节省了29天的磨削时间,设置俄罗斯横向长度记录

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To effectively drain the reservoir formations in a Caspian Sea field from a single offshore ice-proof stationary platform (MLSP), the operator wanted to geosteer extended reach 8?-in (215.9 mm) lateral wellbores at maximum ROP and TD in one run. Development of Korchagina field would require several ERD horizontal wells with step-outs up to 8,000 m. The shallow true vertical depth (TVD) of the reservoir combined with low formation strength of the reactive shale requires high mud weight for stability creating a narrow equivalent circulating density (ECD) window. The hydrocarbons are trapped in an anticlinal feature with 70 m of natural gas cap rimmed by 20 m of viscous oil. To avoid early gas production that would lead to catastrophic water break-through, it is critical to keep the horizontal borehole in a narrow vertical corridor of 4-5 meters TVD to ensure maximum oil recovery. To accomplish the objectives would require the latest methods/technologies and would have to adhere to stringent environmental regulations. Using an FEA-based design platform, a BHA solution was developed that contained a 716 type PDC bit fitted with premium 16mm cutters followed by a rotary steerable system (RSS) with an 8 3/8-in (212.7 mm) integral blade stabilizer and 6 3/4-in (171.4 mm) flex collar to enhance directional control. A new oil-based mud would be used to reduce friction factor/wiper trips and stabilize the reactive shale stringers that caused problems when rotating/sliding in offset wells drilled with water-based mud. To fully exploit the integrated BHA’s technological advantage would require establishing a defined set of best practices. In extended reach drilling it is important to monitor torque and drag trends to continuously analyze hole conditions to optimize connections and reduce trip time. Engineers determined that using relatively high pipe rotation (120-180 RPM) would maximize ROP and also enhance removal of drilled cuttings from the low side of the lateral hole section. The drilling team also recognized that reducing connection time is just as important as maximizing ROP because it can account for up to 40% of total drilling hours. To ensure efficient tool make-up, the number of pipe reciprocations was based on modeled torque/drag values enabling engineers to evaluate each stand to effectively manage circulating time prior to setting the slips. Applying the integrated BHA solution and best practices on well P-116 drilled the lateral hole section at 55m/hr, a 62% increase compared to the best offset ROP of 34m/hr, setting a new 24-hr project drilling record of 691m/day. The reliable 6?-in RSS operated flawlessly for 154 hrs exceeding operator expectations. The 8?-in 716 PDC bit displayed good directional control and came out of the hole in acceptable dull condition. The use of oil-based mud successfully stabilized the problematic reactive shale formations and enabled the operator to drill a long open-hole section of 3,770 m in one run setting a new Russian 8?-in horizontal length record. The combination of technologies and expertise completed the well 29 days ahead of schedule. With a spread rig rate of $340,000 cost savings was calculated at approximately $10 million USD.
机译:从单一的海上冰防固定平台(MLSP)有效地排出在里海字段储层地层中,操作者想地质导向伸出距离8?-in(215.9毫米)在最大ROP分支井筒和TD在一次运行。 Korchagina领域的发展将需要与步奏几个ERD水平井高达8000米贮存器与反应性页岩的低地层强度组合的浅真实垂直深度(TVD)需要高泥浆重量为稳定性创建窄等效循环密度(ECD)窗口。烃被捕获在一个背斜特征与天然气帽为70μm由20米粘性油的镶边。为了避免早期的天然气产量,这将导致灾难性水突破,关键是要保持水平井在4-5米TVD狭窄的垂直走廊以确保最大的原油采收率。为了实现目标需要的最新方法/技术,就必须坚持严格的环保法规。使用基于有限元分析的设计平台,BHA溶液开发了含有716型PDC钻头安装有收费16毫米切割器接着是旋转导向系统(RSS)与8 3/8-在(212.7毫米)整体刀片稳定剂和6四分之三英寸(171.4毫米)柔性轴环,以提高方向控制。一种新的基于油的泥浆将用于降低摩擦系数/刮水游和稳定反应性页岩纵梁造成问题旋转时/在邻井滑动水基泥浆钻出的。为了充分利用集成的BHA的技术优势将需要建立一个定义的一组最佳实践。在延伸钻井它来监测扭矩和阻力的趋势连续分析孔条件下优化的连接,并减少行程时间是很重要的。工程师确定使用相对高的旋转管(120-180 RPM)将最大化ROP,并且还从横向孔部的低压侧增强去除钻屑的。钻探队也认识到,减少连接时间,因为它可以占到总钻孔小时到40%是一样重要最大化ROP。为了确保高效的工具化妆,管往复运动的次数是基于模拟扭矩/阻力值,使工程师能够每台机架评估,以有效地管理设置单之前,循环时间。应用集成BHA溶液和最佳实践上以及P-116钻孔在55米/小时的侧孔部,增加了62%,较34米/ hr的最佳偏移ROP,设定691米的新的24小时项目钻孔记录/日。可靠的6?-in RSS完美运行了154个小时,超出运营商预期。 8?-in 716 PDC钻头显示良好方向控制和排在可接受的平淡条件孔出来。使用油基泥浆的成功企稳有问题的反应页岩地层并启用运营商钻3,770米长裸眼井段在一次运行中创下了新的俄罗斯8?-in水平长度纪录。的技术和专业知识相结合,完成了井提前29天。随着$ 340,000节约成本的传播速度钻机在约1000万$美元计算。

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