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Practice of Fuzzy-Ball Drilling Fluid Technology in Qinping CBM Well 12-11-3H with Six Branch Holes

机译:秦平CBM井12-11-3h模糊球钻井液技术的实践

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The 3# high rank coal in Qinshui basin frequently takes place of falling block, sloughing hole, leaking and pipe-stuck during drilling operation. The third open of 12-11-3H well in Qinping is consist of 2 main-branch and 6 sub-branch, using fuzzy-ball drilling fluid for 3 days accomplishing a footage of 4189.49 m. In order to adjust performance of drilling fluid, mix 4 fuzzy-ball drilling fluid additives SDS, SDBS, HES PAM together according to different well condition. The density of this drilling fluid is from 0.96 to 1.08 g/cm~3. The plastic viscosity of it is from 7 to 17 m Pa·s, the yield value is from 4.0 to 10.22 Pa. After using this fuzzy-ball drilling fluid, the drilling rate has increase to 95%, completing the geological demand with an average drilling rate of 12.65 m/h. Compared with adjacent well, the drilling rate has been raised 11.55% with no serious falling block, sloughing or leaking in whole well. However the solid control equipments still need to be strengthened for further improving drilling rate and economic benefits.
机译:秦水盆地3#高排名煤经常发生下降块,脱落孔,在钻孔操作期间泄漏和管道。秦平12-11-3H井的第三个开放由2个主分支和6个子分支组成,使用模糊球钻井液3天完成4189.49米的镜头。为了调节钻孔的性能,混合4个模糊球钻井液添加剂SDS,SDBS,HES PAM根据不同的井条件。该钻井液的密度为0.96至1.08g / cm〜3。它的塑料粘度为7至17 m Pa·s,屈服值为4.0至10.22 pa。使用这种模糊钻孔液体后,钻井率增加到95%,平均完成地质需求钻井率为12.65米/小时。与邻近井相比,钻井率已经提高了11.55%,没有严重的下降块,脱落或泄漏。然而,需要加强固体控制设备,以进一步提高钻井率和经济效益。

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