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Single-Stage Chemical Treatment for Oil-Based Mudcake Cleanup: Field Case and Laboratory Studies

机译:油基泥膜清理的单级化学处理:现场案例和实验室研究

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Formation damage minimization and removal are important factors in enhancing field productivity and achieving targeted production rate. While formation damage is anticipated during drilling, an effective wellbore cleanup fluid becomes essential to remove mud damage and enhance well productivity. Filter cake layer created by drilling fluid can impair production considerably and should be removed prior to production using an effective treatment. Filter cake can be removed using a chemically designed filter cake removal treatment. The design of the treatment requires considerations of mud type and reservoir conditions. Also, it is important to consider the compatibility aspect of the treatment fluid with formation fluids and drill-in fluid base oil. Incompatible fluids result in precipitation which leads to further formation damage. In Saudi Arabia, many sandstone reservoirs are drilled with invert emulsion drill-in fluid to avoid the risk of clays swelling, which can lead to hole sloughing and formation damage. However, production impairment due to mud damage effect was observed in some horizontal wells drilled with invert emulsion drill-in fluid and completed with stand-alone screens as a result of improper mud managemet. After being put on production, their production rates have been reduced significantly with time. The decrease in production was related to screen blockage and mud cake impairment. A newly developed single-stage treatment was spotted and soaked to remove oil based mud cake and screen blockage. A significant sustained improvement in production was noticed and flowback solids indicated removal of screen blockage and mud cake. Lab studies were conducted at reservoir simulated conditions to evaluate the effectiveness of the treatment. The study covered testing the treatment filter cake removal efficiency, return permeability tests with reservoir core samples, and compatibility tests with formation fluids and drill-in fluid base oil. This paper will discuss in detail the laboratory work conducted and the successful field treatment performed.
机译:形成损坏最小化和去除是提高现场生产力和实现目标生产率的重要因素。虽然在钻井期间预期形成损坏,但有效的井筒清洁流体变得必不可少,以消除泥浆损坏并提高良好的生产率。通过钻井液产生的滤饼层可以大大损害生产,并且在生产之前应该使用有效处理在生产之前除去。滤饼可以使用化学设计的滤饼去除处理除去。治疗的设计需要考虑泥浆型和储层条件。而且,重要的是要考虑处理流体的相容性方面与地层流体和钻孔流体基础油。不相容的液体导致沉淀,导致进一步的形成损伤。在沙特阿拉伯,许多砂岩储层用逆变乳液钻孔钻井钻孔,以避免粘土膨胀的风险,这可能导致孔脱落和形成损坏。然而,在一些水平孔中观察到由于倒置乳液钻头流体钻孔的泥浆损伤引起的生产损伤,并且由于泥浆管理不当而与独立屏幕完成。经过生产后,随着时间的推移,它们的生产率显着降低。生产减少与屏幕堵塞和泥蛋糕损伤有关。发现了新开发的单级处理,浸泡并浸泡以去除油基泥饼和筛网堵塞。注意到生产的显着持续改善和流量固体表明筛选屏幕堵塞和泥饼。在储层模拟条件下进行实验室研究,以评估治疗的有效性。该研究涵盖了检测处理过滤滤饼去除效率,用储层核心样品返回渗透性试验,以及具有地层流体和钻孔流体基础油的相容性测试。本文将详细讨论进行的实验室工作,并进行成功的现场治疗。

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