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LUBE OIL IN ETHYLENE REFRIGERATION MACHINE

机译:乙烯制冷机中的润滑油

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Following a plant turnaround in mid-2007, the ethylene refrigeration compressor was restarted. During restart, the compressor began to surge. The compressor was shut down due to high amps with an apparent seal failure. The older design of the wet seals allowed approximately 400 gallons of lube oil to leak into the refrigeration system. The seal was replaced and the majority of this oil was removed using a toluene wash followed by several washes with a mix of n-propanol and methanol. The compressor was restarted without issue and ran nine months until a power failure tripped the plant. During the power failure the refrigeration system warmed allowing the stagnant oil to move into undesired locations. Upon startup, the plant experienced poor heat transfer and high pressure drop in the cold box. This resulted in heavy ethylene losses from the demethanizer, and below target production due to pressure drop concerns. When normal operating conditions could not be met the refrigeration system was warmed and cleaned using toluene to disperse the oil and chased with methanol several times. This effort had little effect on improving heat transfer in the cold box. The plant was shut down to inspect the demethanizer and clean the cold box. During this shutdown the first, second, third stage suction drums and demethanizer condenser were cleaned by circulating toluene and chased with methanol. The plant was brought online and heavy losses to fuel were still occurring. To help increase heat exchange an additional exchanger was put online. This exchanger has cracked gas on the tube side and ethylene refrigeration on the shell side. Using this exchanger cooled the demethanizer feeds resulting in better tower performance and lower pressure drop. For weeks following this restart of the compressor, the shell side of the exchanger was blown down several times a shift to remove any oil. This greatly improved heat transfer in the cold box, but did not restore optimal performance. The plant continues to operate with lower heat transfer in the cold box and higher than normal losses to fuel. Several actions were taken to reduce the potential for this failure during startup. Startup procedures were revised to ensure the seal pots are unblocked when putting compressor oil system into service and starting the refrigeration compressor. A shutdown strategy was developed to prevent damage due to prolonged compressor surging. The attempts to remove the oil resulted in increased downtime and loss of production. This paper will further describe the mechanisms of failure and provide more detail on the activities taken to remedy the problem and concepts to reduce the severity.
机译:在2007年中期的植物周转之后,重新启动乙烯制冷压缩机。在重启期间,压缩机开始激增。由于高安培而关闭压缩机,具有表观密封率。湿密封的旧设计允许大约400加仑的润滑油泄漏到制冷系统中。替换密封件,并使用甲苯洗涤后除去大部分油,然后用N-丙醇和甲醇混合洗涤几次。在没有问题和九个月的情况下重新启动压缩机,直到电源故障绊倒植物。在电源故障期间,制冷系统温热允许停滞的油进入不希望的位置。启动后,植物在冷箱中经历了差的传热和高压下降。这导致脱甲烷的重质乙烯损失,并且由于压降问题导致目标产量低于目标产量。当无法满足正常操作条件时,使用甲苯将制冷系统加热并清洁,以分散油并多次捕获甲醇。这项努力对改善冷箱的热传递几乎没有影响。该植物被关闭以检查脱甲烷并清洁冷箱。在该关闭期间,通过循环甲苯并追加甲醇,清洁第一,第二,第三阶段吸管和脱甲烷化剂冷凝器。该植物被带入网上,并仍然发生重大损失。为了帮助增加热交换,将额外的交换机放在网上。该交换器在管侧和壳侧上的乙烯制冷裂化了气体。使用该交换器冷却了脱甲烷饲料,导致塔式性能更好,降低压降。在这次重启压缩机后几周,交换器的壳侧吹出几次移位以去除任何油。这种大大改善了冷箱的热传递,但没有恢复最佳性能。该工厂继续在冷箱中的热传递较低,高于燃料的正常损失。采取了几种行动来减少启动期间此失败的可能性。修改了启动程序,以确保将压缩机油系统投入使用并开始制冷压缩机时,密封罐被拆开。开发了一个关闭策略,以防止由于长时间压缩机飙升而损坏。消除油的尝试导致了增加的停机时间和生产损失。本文将进一步描述失败的机制,并提供更多关于所采取的活动的详细信息,以纠正问题和概念以减少严重程度。

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