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PCCP Sewerage Force Main Structural Condition Assessment and Asset Management Approach

机译:PCCP污水率主要结构条件评估和资产管理方法

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The Greater Lawrence Sanitary District (GLSD) learned in 2002 that Prestressed Concrete Cylinder Pipe (PCCP) supplied to GLSD in 1974, was similar to pipelines experiencing a high rate of catastrophic failures throughout the United States. The District began an assessment program in 2005 to assess the structural condition of one of its PCCP lines. This paper discusses the approach GLSD used to assess the structural condition of the pipeline, including finite element analysis, acoustic and transient pressure monitoring, electromagnetic inspection, visual and sounding inspection, and material testing. This paper also discusses the emergency structural repair that was accomplished when one pipe section was found to be in imminent danger of failure. GLSD treats wastewater from Lawrence, Methuen, Andover and North Andover Massachusetts and Salem New Hampshire. The design capacity of the GLSD treatment plant is 52 MGD. During wet weather, the flow is increased to 110 MGD. Current plans involve raising the peak wet weather capacity of the plant to 135 MGD and in the future to 165 MGD. GLSD owns over 4 miles of PCCP ranging from 48 to 102 inches in diameter, which was manufactured by Interpace Corporation in 1973 and 1974. Much of this pipe is used in lower pressure applications. However, one GLSD pipeline, the Riverside Pump Station (RPS) 2700 foot long 72 inch diameter force main operates at higher pressures. Virtually all sewage received by GLSD is pumped to the treatment plant through the RPS force main. The force main route is through a residential neighborhood and crosses under an active railroad track that is used by Amtrak, commuter trains and freight trains. The majority of the force main is between 200 feet and 1000 feet from the Merrimack River, a major recreational, water supply and fisheries resource. Failure of this pipeline would have significant financial, environmental and operational consequences.
机译:2002年的大劳动卫生区(GLSD)于2002年了解到,1974年提供给GLSD的预应力混凝土气缸管(PCCP)类似于在美国整个美国经历高灾难性失败的管道。该区于2005年开始评估课程,以评估其PCCP线的结构状况。本文讨论了用于评估管道结构状况的方法GLDSD,包括有限元分析,声学和瞬态压力监测,电磁检测,视觉和探测检查和材料测试。本文还讨论了当发现一个管道部分迫在眉睫的失败危险时完成的紧急结构修复。 GLSD将废水从劳伦斯,甲特酮,南侧和北坡马萨诸塞州和塞勒姆新罕布什尔郡享用废水。 GLSD治疗厂的设计能力为52 MGD。在潮湿的天气期间,流量增加到110 mgd。目前的计划涉及将工厂的峰值潮湿天气容量提高到135 MGD,并将来为165 MGD。 GLSD拥有超过48英寸的直径,由48至102英寸的直径,由1973年和1974年由Interpace Corporation制造。大部分管道用于较低压力应用。然而,一个GLSD管道,滨江泵站(RPS)2700英尺长的72英寸直径力主要在更高的压力下操作。实际上,GLSD接收的所有污水通过RPS力主要泵入处理厂。力主要路线是通过住宅邻居,并在Amtrak,Commuter火车和货运列车使用的有源铁路下交叉。大多数力量主要距离Merrimack河,主要的娱乐,供水和渔业资源之间200英尺和1000英尺。该管道的失败将具有重大的财务,环境和运营后果。

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