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Continual Bit Design Evolution Improves Performance in the Skinner Ridge Field - Piceance Basin

机译:持续的位设计进化提高了Skinner Ridge Field的性能 - Piceance盆地

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The Piceance Basin is one of several unconventional gas resources that have been the subject of intense industry activity throughout onshore North America. Due to challenged Rocky Mountain natural gas prices and a recent high cost environment, drilling and completing wells quickly and inexpensively is crucial to managing the economic conditions in Chevron’s Skinner Ridge Field development in western Colorado. A focused effort on continual improvement has been employed by the Chevron Piceance Drilling Team to maximize drilling efficiency. In terms of drilling performance, an obvious method to reduce drilling time and cost is to physically drill faster by achieving increased drill bit rate of penetration (ROP) without compromising bit reliability. The following paper summarizes performance improvements achieved through numerous bits trials, dull bit grading analyses and design iterations through a process of application design engineering at the supplier/customer interface. The result has been a step change in drill bit performance exhibited by the continual increase in average 7-7/8 inch bit ROP: from 45 ft/hr during the initial delineation program to 184 ft/hr on the most recent development well pad. Based on this demonstrated performance, the bit designs and cutter technologies have been transferred to other operations, showing that the application of this design approach provides practical means of maximizing efficiency.
机译:Piceance盆地是几种非传统气体资源之一,这是整个北部北美剧烈行业活动的主题。由于挑战的岩石山天然气价格和最近的高成本环境,钻探和完成井的速度迅速,廉价地为在科罗拉多州西部的雪佛龙皮肤岭野外发展中管理经济状况至关重要。 Chevron Piceance钻探团队雇用了一项持续改进的一项集中努力,以最大限度地提高钻井效率。在钻井性能方面,通过在不影响比特可靠性的情况下,通过实现增加的钻头(ROP)的钻头比率(ROP)来物理钻取更明显的方法。下文通过供应商/客户界面的应用设计工程过程,总结了通过众多比特试验,沉闷的比特分析和设计迭代来实现的性能改进。结果一直是钻头性能的一步变化,在初步描绘计划期间平均持续增加7-7 / 8英寸比特ROP:从最近的开发井垫上的184英尺/小时,从45英尺/小时。基于这一说明的性能,位设计和刀具技术已被转移到其他操作,表明这种设计方法的应用提供了最大化效率的实用手段。

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