首页> 外文会议>20th International North Sea Flow Measurement Workshop; Oct 22-25, 2002; St Andrews Bay Resort, Scotland >Analysis and Elimination of Disturbing Flowrates Deviations Between a 24' ANSI 600 Ultrasonic Meter and Vortex Meter in a Natural Gas Meter Station
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Analysis and Elimination of Disturbing Flowrates Deviations Between a 24' ANSI 600 Ultrasonic Meter and Vortex Meter in a Natural Gas Meter Station

机译:天然气计量站中24“” ANSI 600超声波仪表和涡街流量计之间干扰性流量偏差的分析和消除

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During the startup phase of a newly erected meter station for natural gas, considerable synchronism deviations were discovered between the ultrasonic and vortex meters arranged in series. In order to eliminate the difference, the inlet zone of the meters was extended by 40 D, among other things, and a second high pressure test was carried out for both meters. The renewed high pressure test showed for the ultrasonic meter a shift of 0,5% for which there is no explanation up to the present day, and this leads to a corresponding reduction of the synchronism difference. The extension of the inlet failed to produce any improvement. The synchronism quality of the measuring devices continued to be unacceptable. With the additional installation of a turbine meter, the vortex meter was positively identified as being the primary source of the shift. At the same time, a dependence of the synchronism on the position of the control ball valve located approx. 50 D downstream was determined. As verified by a detailed pulsation measurement, there is a systematic correlation between the differential pressure across the control ball valve, the stochastic pressure and velocity fluctuations within the measuring section as well as the synchronism deviation between the ultrasonic and vortex meters. Evidently, an increase of the flow turbulence at the vortex meter at constant volume flow led to a reduced indication. The vortex shedding frequencies (Strouhal number) decrease at constant Reynold's number with increasing turbulence (intensity and coherence length, respectively). As a remedial action, the control ball valve was equipped with two multi-hole discs so that the natural gas for expansion no longer has to flow through one cross-section but rather through a multitude of boreholes. In this case, the number of boreholes as well as the borehole diameters increase in amount and size with the increasing opening phase of the control ball valve. With this remedial action, the stochastic fluctuations in the natural gas flow were reduced significantly. At the same time, the synchronism between the vortex meter and the ultrasonic meter was improved significantly and was subsequently accepted by all participants.
机译:在新建的天然气计量站的启动阶段,超声波和涡旋流量计串联后发现了相当大的同步偏差。为了消除这种差异,仪表的入口区域尤其扩大了40 D,并对这两个仪表进行了第二次高压测试。重新进行的高压测试表明,超声波仪表的位移为0.5%,迄今为止尚未有任何解释,这导致同步差的相应降低。入口的扩展无法产生任何改善。测量设备的同步质量仍然不能令人满意。通过额外安装涡轮流量计,旋涡流量计被肯定地确定为该换档的主要来源。同时,同步对控制球阀的位置的依赖性约为。确定下游50D。如通过详细的脉动测量所证实的,在控制球阀两端的压差,测量部分内的随机压力和速度波动以及超声波和涡流计之间的同步偏差之间存在系统的相关性。显然,在恒定体积流量下在涡流计处的湍流增加导致指示减小。涡旋脱落频率(斯特劳哈尔数)在恒定的雷诺数下随着湍流(强度和相干长度)的增加而降低。作为补救措施,控制球阀配备了两个多孔盘,因此,用于膨胀的天然气不再必须流经一个横截面,而要流经多个钻孔。在这种情况下,随着控制球阀的打开相位的增加,孔的数量以及孔的直径在数量和尺寸上都增加。通过这种补救措施,天然气流量的随机波动显着减少。同时,涡流计和超声波计之间的同步得到了显着改善,随后被所有参与者接受。

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