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Ultra-Low NOx Gas Turbine Combustor. Final Report, October 1985-June 1990

机译:超低NOx燃气轮机燃烧室。最终报告,1985年10月至1990年6月

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The design and rig testing of a lean premixed, low emissions, gas turbinecombustor prototype are described. The combustor evaluated was a 90 degree sector of a full-scale annular combustor for a 3.7 Mw, natural gas-fired, industrial gas turbine. The combustor sector represented an intermediate development step in extending the lean premixed combustor technology from a can combustor configuration with a single fuel injector to an annular geometry with multiple injectors. In a parallel effort, a rich/lean combustor sector was also evaluated. This effort provided a direct comparison of the NOx reduction capabilities of the rich/lean and lean premixed concepts. Testing at typical gas turbine operating pressures (122 psig) demonstrated that both the lean premixed and rich/lean combustor sectors were capable of meeting the program NOx goal of 25 ppm (15% O2) while maintaining CO emissions below 50 ppm. The testing indicated that variable geometry and fuel staging will be required for low emissions range extension and low part load operation, respectively.

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