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Failure investigation of a drilled shaft stabilised slope

机译:钻孔竖井稳定边坡的破坏研究

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摘要

In this paper, failure of a drilled shaft stabilised slope during basement excavation of an office building in Taipei city, Taiwan, is investigated. Four and two stages of excavation along the respective east and west sides of the site were planned. A row of drilled shafts was installed along each side before excavation. Severe slope movement occurred and extended outside the project area on both sides during excavation due to a weak clay layer overlying bedrock, unpredicted local trough between the soil/rock interface and improper design of the drilled shafts. Study of the possible reasons for failure includes monitoring results evaluation and numerical studies by means of the computer code Plaxis.
机译:本文研究了台湾台北市一栋办公楼地下室开挖过程中钻孔竖井稳定边坡的破坏情况。计划在该场地的东侧和西侧分别进行四个和两个阶段的开挖。开挖前,沿每一侧都安装了一排钻探井筒。由于在基岩上覆盖着一层薄弱的粘土层,土壤/岩石界面之间的不可预料的局部低谷以及钻探井的不适当设计,在开挖过程中发生了严重的斜坡运动,并在两侧超出了项目区域。对故障可能原因的研究包括监视结果评估和通过计算机代码Plaxis进行的数值研究。

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