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首页> 外文期刊>Model engineers' workshop >Brian Wood's Dore Westbury Mk Ⅱ Miller
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Brian Wood's Dore Westbury Mk Ⅱ Miller

机译:布莱恩·伍德的多尔·韦斯特伯里MkⅡMiller

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Photograph 14 shows the head thus supported leaving a void where the support used to be. Also visible top left in this photo is the shim, coloured blue for 0.003 inches thickness, on the face of the uppermost packing slab. Photograph 15 is an inside view of the capstan after 9 years of service, but what cannot be seen and came as a bad shock was the state of the key, which is seen here in photo 16. It was made in silver steel, hardened and tempered as directed in the build notes but clearly the loading has been too much for the design in that form and it was cracked right through with maybe only 45% of it left on the remaining side doing any useful work. Returning to the motor drive, I was keen to avoid the risk of powering up the lift motor when the column was clamped, so I built in an interlock to isolate the motor while the column was clamped. A flat was milled across the plain section of the lower clamp bolt to activate a proximity switch that was wired to isolate the live feed to the motor while the column is clamped. Photograph 17 shows this part of the installation. Two further precautions were taken against accidental power application by first unplugging the power lead when height adjustment was no longer needed and secondly by getting into the habit of leaving the change over switch in the central OFF position I accept that with two clamp bolts it is not a completely fail safe situation, but with just myself using the mill I considered those precautions would be quite adequate. Even if a senior moment were to take place, it would be realised immediately and the power cancelled, with words like 'tut tut' being used. Photograph 18 shows the gearing arrangement from the motor to the capstan. The lock down bolt, with the short tommy bar, to clamp the swing away idler gear carrier can also be seen here.
机译:照片14显示了这样支撑的头部,在以前的支撑位置留下了空隙。在这张照片的左上方还可以看到垫片,该垫片在最上面的包装平板的表面上呈蓝色,厚度为0.003英寸。照片15是使用了9年的绞盘的内部视图,但无法看到,但受到严重震动的是钥匙的状态,在照片16中可以看到。它是由银色钢制成,经过硬化处理,按照构建说明中的说明进行了调和,但显然,对于这种形式的设计而言,负载已太多了,并且完全破裂了,剩下的一侧可能只有45%可以做任何有用的工作。回到电动机驱动器,我渴望避免在夹住色谱柱时为提升电机通电的风险,因此我建立了一个互锁装置,以在夹住色谱柱时隔离电动机。在下部夹紧螺栓的平面上铣削一个平面,以激活一个接近开关,该开关已接线,可在夹紧色谱柱时隔离带电的电动机。照片17显示了安装的这一部分。采取了两项预防意外电源的预防措施,首先是在不再需要高度调节时拔下电源线,其次是养成将转换开关保持在中间OFF位置的习惯,我接受有两个夹紧螺栓的情况完全失败的情况,但是仅凭我自己使用磨机,我认为这些预防措施就足够了。即使发生了重要的时刻,也将立即意识到并取消了电源,并使用了“ tut tut”之类的字眼。照片18显示了从电动机到绞盘的齿轮传动装置。在这里还可以看到带有短的汤姆棒的锁定螺栓,用于夹紧摆动的惰轮支架。

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