首页> 外文期刊>Journal of Hydraulic Engineering >Bridge Blockage and Overbank Flow Simulations Using HEC-RAS in the Keelung River during the 2001 Nari Typhoon
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Bridge Blockage and Overbank Flow Simulations Using HEC-RAS in the Keelung River during the 2001 Nari Typhoon

机译:2001年纳里台风期间在基隆河上使用HEC-RAS进行的桥梁堵塞和河床溢流模拟

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摘要

On September 16, 2001, Typhoon Nari resulted in severe flooding in the Keelung River basin. More than 1,000 shipping containers were swept by the rising water from the floodplain into the river, blocking 14 bridges. A severe overbank flow due to the blockage occurred at the Ba-Tu Railway Bridge. The overbank flow then passed through a railway tunnel and inundated Keelung City, resulting in significant damage. The objective of this study was to determine the influence of the bridge blockage and the Ba-Tu overbank flow on the water stages in the Keelung River during Typhoon Nari. The floating-pier-debris module and the lateral-weir module in the Hydrologic Engineering Center-River Analysis System (HEC-RAS) unsteady-flow routing model were applied to investigate water stage variation due to the bridge blockage and overbank flow. The numerical simulation results provided by this study served as an important reference for authorities who needed to clarify the responsibility of the containers' owners for the loss of lives and property during this typhoon.
机译:2001年9月16日,纳里台风在基隆河流域造成严重洪灾。从洪泛区到河中的上升水淹没了1,000多个集装箱,堵塞了14座桥梁。由于巴图铁路桥的堵塞,导致严重的堤岸流量。然后,过多的资金流通过铁路隧道并淹没了基隆市,造成了严重破坏。这项研究的目的是确定台风纳里期间,桥梁阻塞和Ba-Tu过高流量对基隆河水位的影响。应用水文工程中心河水分析系统(HEC-RAS)非恒定流路径模型中的浮码头-泥石模块和侧堰模块,研究由于桥​​梁阻塞和过高流量引起的水位变化。这项研究提供的数值模拟结果为有关当局提供了重要参考,这些当局需要澄清集装箱所有者在此次台风期间对人员伤亡和财产损失的责任。

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