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Analysis and Research on Pipeline Vibration of a Natural Gas Compressor Station and Vibration Reduction Measures

机译:天然气压缩机站管道振动分析与研究及减震措施

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摘要

The abnormal vibration of natural gas station pipelines seriously threatens the safety of pipeline transportation, and improper handling will cause huge economic losses. For the abnormal vibration of the pipeline, reasonable treatment must be carried out. The Yongchang gas station belongs to the west-east gas pipeline system in China. Since its production, abnormal vibration has often occurred in the west-third outbound pipeline of the Yongchang gas station, and the vibration changes according to the different gas transport volumes. In this paper, the outbound pipeline of the Yongchang pressure station is taken as the research object, and the vibration analysis of the station yard pipeline is carried out. The numerical model of the station yard pipeline is established, and the correctness of the model is verified by the field vibration test. The fluid-solid coupling method is used to analyze pipeline vibration under different working conditions. Then, three kinds of vibration reduction schemes are proposed and verified by simulation. The main conclusions are as follows: (1) The fluid pressure fluctuation in the pipeline is the root cause of abnormal vibration in the station. (2) When the gas transmission volume is large, the vibration of the pipeline system will become more severe. (3) The scheme of increasing pipe diameter and adding appropriate constraints has the best vibration reduction effect.
机译:天然气站管道的异常振动严重威胁到管道运输的安全性,处理不当会导致巨大的经济损失。对于管道的异常振动,必须进行合理的处理。永昌加油站属于中国西部消气管道系统。由于其生产,在永昌加油站的西第三出站管道中经常发生异常振动,振动根据不同的气体运输量而变化。本文采用了永昌压力站的出站管道作为研究对象,进行了站码管道的振动分析。建立了站围场管道的数值模型,通过现场振动测试验证了模型的正确性。流体固耦合方法用于在不同的工作条件下分析管道振动。然后,通过模拟提出并验证了三种减振方案。主要结论如下:(1)管道中的流体压力波动是车站中异常振动的根本原因。 (2)当气体传动量大时,管道系统的振动将变得更加严重。 (3)增加管道直径和添加适当约束的方案具有最佳减振效果。

著录项

  • 来源
    《Energy & fuels》 |2021年第1期|479-492|共14页
  • 作者单位

    Southwest Petr Univ Petr Engn Sch Chengdu 610500 Sichuan Peoples R China;

    Southwest Petr Univ Petr Engn Sch Chengdu 610500 Sichuan Peoples R China;

    Nat Gas Res Inst Southwest Oil & Gas Field Branch Chengdu 610213 Sichuan Peoples R China;

    Sinopec Petr Engn Zhongyuan Corp Zhengzhou 450000 Henan Peoples R China;

    Cardiff Univ Sch Engn Cardiff CF24 3AA Wales;

  • 收录信息 美国《科学引文索引》(SCI);美国《工程索引》(EI);美国《生物学医学文摘》(MEDLINE);
  • 原文格式 PDF
  • 正文语种 eng
  • 中图分类
  • 关键词

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