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Retrofitting of an Existing Condensate Recovery Plant to Maximize Natural Gas Liquids Production

机译:改造现有的冷凝水回收装置,以最大程度地提高天然气液的产量

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Nowadays, gas processing for NGLs (Natural Gas Liquids) and LPG (Liquefied Petroleum Gas) recovery has gained a great interest due to the increase of the market demand as well as the higher prices of these products. Based on sales gas calorific value from ABU-SANNAN Condensate Recovery Plant (General Petroleum Company-Egypt) and by close monitoring of NGLs content in feed and sales gas, it is clear that there is a valuable amount of NGLs leave with sales gas without recovery. NGLs have significantly greater value as separated products than as part of the gas stream, so General Petroleum Company could seek ways and means to maximize NGLs recovery. The current research work proposes a possible modification of ABU-SANNAN Condensate Recovery Plant to produce liquefied petroleum gas (LPG) from natural gas liquids (NGLs), instead of producing lighter hydrocarbon gases during the stabilization process, in addition to the current condensate and sales gas products. The new LPG recovery unit will comprises of: Molecular Sieve based-dehydration unit, Turbo-Expander unit, Cold Box heat exchanger, DE-ETHANIZER system, DE-ETHANIZER Overhead compressor, DE-BUTANIZER system, and two LPG storage bullets. New process equipment selection, sizing and rating will be performed by using Aspen HYSYS simulation program V8.8. The results show that the retrofitted plant can produce 87 Tons/Day of LPG. The produced LPG can participate to solve the LPG shortage problem in Egypt. The economic evaluation for the Retrofitted Plant is conducted by using Aspen Capital Cost Estimator V8.8, to ensure rapid return of investment and good profitability over the expected lifetime. It is remarkable that the Retrofitted plant has a great value from the economic point of view as the total capital investment will be paid back within two years, so the Retrofitted plant will achieve a high and rapid return on investment (ROI). The efforts done in this work are helpful and can be applied for plants in operation as well as the plants under design for increasing their profits.
机译:如今,由于市场需求的增加以及这些产品的较高价格,NGL(天然气液体)和LPG(液化石油气)回收的气体处理引起了人们极大的兴趣。根据ABU-SANNAN凝析油回收厂(埃及通用石油公司)的销售气体热值,并通过严密监控进料和销售气体中的NGL含量,很明显,有大量有价值的NGL随销售气体一起残留而没有回收。 NGL作为分离产品比作为气流的一部分具有更大的价值,因此通用石油公司可以寻求方法和手段来最大化NGL的回收率。当前的研究工作建议对ABU-SANNAN冷凝水回收厂进行改造,以从天然气液体(NGL)生产液化石油气(LPG),而不是在稳定化过程中生产较轻的烃类气体,除了目前的冷凝水和销售以外气体产品。新的液化石油气回收装置将包括:基于分子筛的脱水装置,涡轮膨胀机装置,冷箱式热交换器,DE-ETHANIZER系统,DE-ETHANIZER架空压缩机,DE-BUTANIZER系统和两个LPG储存子弹。使用Aspen HYSYS仿真程序V8.8将执行新的工艺设备选择,选型和定额。结果表明,改造后的工厂每天可生产87吨LPG。生产的液化石油气可以参与解决埃及的液化石油气短缺问题。使用Aspen资本成本估算器V8.8进行翻新厂的经济评估,以确保在预期的使用寿命内快速获得投资回报和良好的盈利能力。值得注意的是,从经济角度来看,改造后的工厂具有巨大的价值,因为总资本投资将在两年内归还,因此改造后的工厂将获得高且快速的投资回报(ROI)。这项工作所做的努力是有帮助的,可以应用于正在运行的工厂以及正在设计中的工厂,以增加其利润。

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