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Staged Premium Screen Completion Design for Horizontal Well Based on Laboratory Test: A Successful Application in Block 451, Shengli Oil Field

机译:基于实验室测试的水平井分段优质筛网完井设计:在胜利油田451区块的成功应用

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Staged premium screen has been applied to balance the inflow profile of horizontal well under open hole completion in Shengli Oil Field, China. Perforation density of base pipe is the key parameter of staged screen for inflow control, however, it is used to be determined by only considering drawdown due to perforation itself, ignoring two dominant parts caused by formation sand filter cake around screen and sand retention material, therefore the decision plan is not suitable. To solve this problem, a laboratory apparatus was run to test a screen sample, and thoroughly analyzed the effect of perforation density on total inflow control drawdown. A base pipe was also tested, working as a reference to screen sample. The test simulated down hole flowing condition in Well DXY451P21, Block 451, Shengli Oil Field, test results were directly utilized to design staged premium screen for this target well. Finally, the following conclusions can be drawn: pressure drop in screen sample is much sensitive to perforation density, and is obviously larger than that in base pipe sample; flowing pressure is mainly lost in formation sand filter cake and sand retention material, where the flow pattern is seepage flow; perforations on base pipe of premium screen mainly play a part in regulating flowing field, i.e. smaller perforation density will lead produced liquid to flow a longer distance in seepage media and bring a larger additional drawdown; the production performance of Well DXY451P21 is much better than adjacent wells, and promotes economic benefits.
机译:在中国胜利油田裸眼完井下,采用分段溢流筛管来平衡水平井的流入剖面。中心管的射孔密度是分流筛管控制入水的关键参数,但是它仅通过考虑由于射孔本身引起的压降来确定,而忽略了由筛管周围的地层砂滤饼和挡砂材料引起的两个主要部分,因此,该决策计划不合适。为了解决这个问题,运行了一个实验室设备来测试筛网样品,并彻底分析了穿孔密度对总流入控制压降的影响。还对基管进行了测试,作为筛分样品的参考。试验模拟了胜利油田451区块DXY451P21井的井下流动条件,直接将试验结果用于设计该目标井的分段溢流筛。最后,可以得出以下结论:筛网样品中的压降对射孔密度非常敏感,并且明显大于基管样品中的压降。流动压力主要损失在地层砂滤饼和挡沙材料中,其流动方式为渗流。优质筛网基管上的孔眼主要起调节流场的作用,即较小的孔眼密度将导致采出液在渗流介质中流动更长的距离,并带来更大的附加压降; DXY451P21井的生产性能远远优于相邻的井,并具有经济效益。

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