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The Montara oil spill report

机译:蒙塔拉溢油报告

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摘要

On 21 August 2009, a blowout occurred on the HI well of the Montara Wellhead Platform.1 On the same day, all 69 personnel of the platform were safely evacuated.2 The most likely cause of the blowout was the failure of the primary well control barrier (a cement shoe casing).3 Further, only one of two planned secondary well control barriers (pressure containing anti-corrosion caps) had been installed.4 Following the blowout, oil began to leak into the sea. The rate of discharge was initially estimated at 400 barrels a day, though it may have reached 1500 barrels.5 Estimates of the resulting surface sheen ranged from 6000-25,000 square kilometres.6 The discharge was finally stopped in November 2009, when the well's operator, PTTEP Australasia (Ashmore Cartier) Pty Ltd (PTTEPAA), successfully drilled a relief well (after several failed attempts).7 While impacts on islands in the area and the Western Australian coastline were "largely avoided", because of remoteness and a lack of evidence, the exact nature of the environmental impact will never be known.8
机译:2009年8月21日,Montara井口平台的HI井发生井喷。1在同一天,平台上的所有69名人员都被安全疏散。2井喷的最可能原因是主井控制失败屏障(水泥鞋套)。3此外,仅安装了两个计划中的二级井控屏障(压力包含防腐蚀盖)之一。4井喷之后,石油开始泄漏到海中。最初的排放量最初估计为每天400桶,尽管可能达到1500桶。5估计的表面光泽范围为6000-25,000平方公里。6最终于2009年11月停止排放,当时该井的操作员,PTTEP澳大拉西亚(Ashmore Cartier)Pty Ltd(PTTEPAA)成功地钻了一口救援井(经过几次失败尝试)。7由于偏远和缺乏,“很大程度上避免了”对该区域和西澳大利亚海岸线上岛屿的影响有证据表明,环境影响的确切性质永远不会被知道8。

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