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Fast-Track Repair of 42-Inch PCCP Water Main Houston, Texas

机译:快速修复42英寸PCCP水管得克萨斯州休斯敦

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During the early morning hours of June 8, 2004, a prestressed concrete cylinder pipe (PCCP) installed in 1991 through 1992 suffered a catastrophic failure. This failure occurred in a pipe section of existing 42-inch (1,067 mm) water line, which supplies potable surface water to Sims Bayou Pump Station in Houston, Texas. Several residential properties were flooded as a result of the failure. The City of Houston (City) authorized Lockwood, Andrews & Newnam, Inc. (LAN), to assist in the failure assessment and to design the repair for the water line. LAN performed a visual inspection of the water line interior around the failure location, and performed testing on wire and mortar samples. Initial test results and observations of the failed pipe section revealed that severe cracking existed in both mortar lining and coating, the prestressing wire did not exhibit signs of hydrogen embrittlement; however, the wire did exhibit severe corrosion, which may have facilitated the onset of failure. Further inspection revealed that the internal cracking appeared consistently at invert, crown and both springlines for a distance of approximately 26,000 linear feet from the pump station. Due to the risk of collateral damage should a second failure occur, LAN and the City determined that the line would not be placed back in service without extensive rehabilitation. Because this line is the only source of surface water to the area, groundwater wells were brought online. These wells were required to operate at full capacity in order to supply the demand during the outage of the line, and hydraulic modeling indicated that the groundwater wells alone were not sufficient to meet the summer peak water demands in the area. Therefore, LAN and the City were faced with the task of rehabilitating 26,000 linear feet of 42-inch water line and safely returning it to service before Summer 2005. This paper presents the options, cost estimates and schedules evaluated to fast-track the rehabilitation. The evaluation led to the conclusion that the most feasible solution was to perform design to slipline the existing line and provide bid-ready documents within two-months, allowing approximately six months to construct the improvements to the 5 mile stretch of water line. The paper will also discuss some of the lessons learned as the project went to construction.
机译:在2004年6月8日凌晨,1991年至1992年安装的预应力混凝土圆柱管(PCCP)遭受了灾难性的破坏。此故障发生在现有42英寸(1,067毫米)输水管道的管道部分中,该管道向得克萨斯州休斯敦的Sims Bayou泵站提供了饮用水。失败的结果淹没了几处住宅物业。休斯敦市(市)授权洛克伍德,安德鲁斯和纽南公司(LAN)协助进行故障评估和设计供水管线的维修。局域网对故障位置周围的输水管线内部进行了目视检查,并对电线和砂浆样品进行了测试。初步的测试结果和对破裂管段的观察表明,砂浆衬里和涂层都存在严重的裂纹,预应力丝没有显示出氢脆的迹象。但是,电线确实表现出严重的腐蚀,这可能促进了故障的发生。进一步检查发现,在与泵站相距约26,000线性英尺的范围内,内部裂纹始终出现在反向,拱顶和两个弹簧线上。由于如果发生第二次故障可能会造成附带损坏,因此,LAN和纽约市政府决定,如果不进行大规模修复,则不会恢复使用该线路。由于这条管线是该地区唯一的地表水源,因此使地下水井在线。为了在管线中断期间满足需求,这些井必须满负荷运转,并且水力模型表明,仅地下水井不足以满足该地区夏季的高峰用水需求。因此,LAN和纽约市面临的任务是修复26,000线性英尺的42英寸输水管线,并在2005年夏季之前安全地将其重新投入使用。本文介绍了为快速跟踪修复工作而进行的选择,成本估算和时间表。评估得出的结论是,最可行的解决方案是对现有管线进行设计,并在两个月内提供投标准备文件,从而允许大约六个月的时间对5英里长的供水管线进行改进。本文还将讨论该项目进行中的一些经验教训。

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