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ENHANCED PRIMARY TREATMENT: FULL-SCALE PILOT ANSWERS MANY QUESTIONS

机译:增强的主要治疗方法:全面的飞行员答案很多问题

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The King County Wastewater Treatment Division initiated an investigation in 2001 of the potential use of ferric chloride addition for enhanced primary treatment at the South Treatment Plant in Renton, Washington. The South Treatment Plant treats an annual average flow of 70 million gallons per day (mgd). The objective of the study was to determine if the benefits of enhanced solids removals using ferric chloride (FeCl3) for advanced primary treatment (APT) in the primary clarifiers, and resultant energy savings in the secondary and solids processes, outweighed the cost of purchasing ferric chloride and flocculant aid polymer. The project began in March 2001 with jar testing of various doses of ferric chloride and polymer. The target primary clarifier removal rates were 50 percent biochemical oxygen demand (BOD) and 80 percent total suspended solids (TSS). These removal rates were seen during jar testing at doses of 30 mg/L ferric chloride and higher (the stoichiometric demand based on influent phosphorus concentration was approximately 35 mg/L). However, the cost of the chemicals at a dose of 30 mg/L would likely make enhanced primary treatment infeasible. The study initially targeted a dose of 15 to 20 mg/L ferric chloride, with a dose of 0.2 mg/L anionic polymer to see if some enhancement in the removal rates would provide a benefit to the plant operations budget. Two trial periods were planned: one under partial flow conditions (1 to 4 primary clarifiers) and one under full-flow conditions (8 primary clarifiers). The first trial (2 weeks long) performed in July 2001 (using one primary clarifier at a ferric chloride dose of 15 to 20 mg/L) did not show removal rates near the target levels in the primary clarifiers. However, a change in the influent wastewater characteristics negatively affected plant performance overall, including the ferric chloride trial. The plant influent was monitored over the next few months. Once it returned to historically “normal” conditions, another trial would be scheduled. The second trial (Round 2) was run in winter 2001 at the same doses using four clarifiers. The results were near the target levels for BOD and TSS removal. The conclusion of the second trial was to wait until summer 2002 and run a trial. In addition, a series of settling tests indicated that the target removals could be achieved with less chemical addition, but longer settling time.
机译:国王县污水处理部门于2001年启动了2001年潜在使用氯化铁的潜在用途,用于华盛顿伦顿伦顿南部治疗厂的初级治疗。南方治疗厂每天治疗每年7000万加仑(MGD)的年平均流量。该研究的目的是确定使用氯化铁(FECL3)的增强固体去除的益处,用于初级澄清剂中的先进初级治疗(APT),并在二级和固体过程中节省的结果节省,超过了购买铁的成本氯化物和絮凝剂辅助聚合物。该项目于2001年3月开始,罐子测试各种剂量的氯化铁和聚合物。目标初级澄清剂去除率为50%的生化氧需求(BOD)和80%的总悬浮固体(TSS)。在罐子测试期间在30mg / L氯化物的剂量上进行了这些去除率(基于流入的磷浓度的化学计量需求约为35 mg / L)。然而,30mg / L剂量的化学物质的成本可能会产生增强的主要治疗方法。该研究最初靶向15至20mg / L氯化铁的剂量,剂量为0.2mg / L阴离子聚合物,看看拆除率的一些增强是否会对植物运营预算提供益处。计划两次试验期:在部分流动条件下(1至4个初级澄清剂)和全流动条件下的一个试验期(8个主要澄清剂)。在2001年7月进行的第一次试验(2周长)(使用15至20mg / L的氯化铁剂量的一个初级澄清剂)未显示在初级澄清器中靶水平附近的去除率。然而,流水废水特性的变化总体影响了植物性能,包括氯化铁试验。在未来几个月内监测植物流量。一旦它返回历史上“正常”条件,将计划另一次审判。第二次试验(第2轮)在2001年冬季运行,使用四种澄清剂以相同的剂量进行。结果接近靶水平的BOD和TSS去除。第二次审判的结论是等到2002年夏天并进行试验。此外,一系列沉降试验表明,可以通过较少的化学添加,但更长的沉降时间来实现目标去除。

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