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VIBRATION FIELD PROBLEM RESOLVED WITH ANALYTICAL DIAGNOSTICS APPROACH AND INNOVATIVE IMPELLER DESIGN

机译:用分析诊断方法和创新叶轮设计解决了振动场问题

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Several pump units of the same design installed in various locations in the USA with different duties exhibited high vibrations above API limits with process fluids (SG = 0.5 to 0.6) from rated point down to minimum continuous flow. The investigation for root cause was conducted along two parallel paths: experimental and theoretical. On the experimental side a series of shop vibration tests and modal analysis was carried out at full operational speed and cold water (SG = 1.0). These tests included: pump as installed and two modifications of the bearing housings. With the theoretical approach several computer codes of hydraulic analysis were used for analytical diagnosis in order to identify the internal hydraulic phenomena inducing the vibrations. Unsteady hydraulic forces, very likely associated with impeller discharge recirculation, were eventually considered to produce the hydraulic excitation for high vibrations. The strategy for the ultimate solution was based on a new hydraulic design impeller with innovative geometry, I.e., two blade rows with five vanes at inlet and nine vanes at outlet. Shop tests at full operational speed confirmed both the expected pump curve and presented vibrations levels (overall and vane pass) drastically reduced below API limits in the whole operating range, from rated flow down to minimum continuous flow. The new impeller was installed in all sites keeping the existing bearing housings. Field vibration data with the new impeller were collected at different times in a one year period and are compared with data produced by the old impeller. The field vibration levels with the new innovative impeller have been drastically reduced for both the overall amplitude and at vane pass frequency. The key hydraulic design parameter appears to be a high number of vanes at the impeller outlet.
机译:具有不同职责的各种位置的几个具有不同职责的同一设计的泵单元表现出高于API限制的高振动(SG = 0.5至0.6),从额定点降至最小连续流量。根本原因的调查沿两个平行路径进行:实验和理论。在实验侧,通过全操作速度和冷水(SG = 1.0)进行一系列车间振动试验和模态分析。这些测试包括:泵安装和轴承壳体的两个修改。通过理论方法,液压分析的几个计算机代码用于分析诊断,以识别诱导振动的内部液压现象。最终认为不稳定的液压力非常可能与叶轮放电再循环相关,以产生高振动的液压激发。最终解决方案的策略基于具有创新几何形状的新型液压设计叶轮,即两个刀片排,入口处有五个叶片和九个叶片。全部运行速度的商店测试确认了预期的泵曲线和呈现的振动水平(总体和叶片通过)在整个工作范围内大大降低了API限值,从额定流量下降到最小连续流量。新叶轮安装在保持现有轴承座的所有网站中。与新叶轮的场振动数据在一年内不同时间收集,并与旧叶轮产生的数据进行比较。具有新型创新叶轮的田间振动水平对于整体幅度和叶片通过频率而言,已经大幅减少。关键的液压设计参数似乎是叶轮插座上的大量叶片。

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