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Experimental Studies of Reinforced Concrete Column Capacity Affected by Core Drilling

机译:钻孔取芯对钢筋混凝土柱承载力影响的试验研究

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The paper presents the experimental studies of reinforced concrete column (RC column) capacity affected by core drilling. By testing three groups (9 total) of full scale concrete short columns, the experiment demonstrates that the axial compression capacity of RC columns after core drilling is reduced from 5.63% to 22.14% while the ultimate displacement decreases from 1.88% to 26.14%. The behavior of columns is altered from the axial compression failure to a small-eccentricity compression failure. The paper summarizes experiment results, followed by an investigation of the dominant factors, such as column effective cross section, drilling location, drilled hole repairing and reinforcing steels discontinued by drilling, that have impact on RC column capacity. The rationale of capacity variations of RC columns due to core drilling is also investigated.
机译:本文介绍了受岩心钻进影响的钢筋混凝土柱(RC柱)承载力的试验研究。通过测试三组(总共9个)全尺寸混凝土短柱,实验证明,取芯后RC柱的轴向抗压能力从5.63%降低到22.14%,而极限位移从1.88%降低到26.14%。圆柱的行为从轴向压缩破坏变为小偏心压缩破坏。本文总结了实验结果,然后研究了影响钢筋混凝土柱承载力的主要因素,例如柱有效截面,钻孔位置,钻孔修复和因钻探中断的钢筋。还研究了由于岩心钻探而引起的RC柱容量变化的基本原理。

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