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Non Process Element Control in the Liquor Cycle Through the Use of an Ash Leaching System

机译:通过使用灰分浸出系统控制白酒循环中的非过程元素

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To improve run-time between washes and reduce thermal cycling of recovery boilers, the Evadale, Texas mill has been attempting to reduce the levels of non-process elements (NPE) in the liquor cycle. The mill has periodically purged electrostatic precipitator ash in an effort to reduce and control concentrations of potassium and chlorides. An additional effort to lower chloride concentrations was made by changing the make-up chemical from diaphragm to membrane grade caustic. Improvements were also made in the operation of the chlorine dioxide generator spent acid salt filter. The change in makeup chemical NPE content successfully reduced the amount of boiler pluggage due to sticky ash formation, but did not allow the desired amount of time between boiler washes. In an effort to further reduce the amount of potassium and chloride in the liquor cycle, an ash leaching system was installed. The leaching system partially dissolves precipitator ash in hot water. The potassium and chloride are selectively leached into the liquid phase and remain in solution. The sodium sulfate crystals are separated from the leaching slurry using a decanting centrifuge and returned to the liquor cycle via a mix tank. The potassium and chloride rich liquid is sewered. Since the implementation of these non-process element reduction methods, the chloride content in the incoming electrostatic precipitator ash has been reduced by roughly 55% and the potassium content has been reduced by about 50%. Approximately 80% of the soda entering the ash leaching process is recovered into the liquor cycle.
机译:为了改善洗涤之间的运行时间并减少回收锅炉的热循环,德克萨斯州伊瓦代尔工厂一直在尝试减少白酒循环中非工艺元素(NPE)的水平。该工厂定期清除静电除尘器灰,以减少和控制钾和氯化物的浓度。通过将补充化学品从隔膜更改为膜级苛性碱,还做出了其他努力来降低氯化物浓度。二氧化氯发生器用过的酸性盐过滤器的操作也得到了改进。补充化学NPE含量的变化成功地减少了由于粘灰形成而导致的锅炉堵塞量,但在锅炉清洗之间没有所需的时间间隔。为了进一步减少液体循环中钾和氯化物的量,安装了一个灰分浸出系统。浸出系统将沉淀灰分部分溶解在热水中。钾和氯化物被选择性地浸入液相中并保留在溶液中。使用倾析离心机将硫酸钠晶体从浸出浆液中分离出来,并通过混合罐返回到液体循环中。排入富含钾和氯化物的液体。由于实施了这些非过程元素还原方法,进入的静电除尘器灰分中的氯化物含量已降低了约55%,钾含量已降低了约50%。进入灰分浸出过程的苏打粉大约有80%被回收到液体循环中。

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