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Power Cost Reduction Through Advanced Quality Control and Refiner Segment Change at Tembec Pine Falls

机译:通过Tembec Pine Falls的高级质量控制和磨浆机部门变更来降低电力成本

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In late 2004 the Tembec Pine Falls mill, teamed up with Metso's Paper and Automation divisions to achieve optimal refining performance by consistently producing high quality pulp with minimal power costs. These objectives required the implementation of advanced controls and real time optimization technologies combined with refiner segment configuration changes on the mainline refiners to prove the concept and measure the savings contribution of the segments and controls independently. As significant energy savings and a large reduction in pulp quality variability were accomplished and sustained, the mill decided to proceed with a permanent installation of the main line system and extended the controls and optimization to incorporate screening and reject refining. A mill peak power control and optimization module was also implemented to optimize operations by managing total mill power and peak load. Four key mechanisms for energy cost reduction were utilized during the project: 1. Specific energy reduction through: 1.1 freeness target shift (possible due to variability reduction), 1.2 optimization of refiner operation (accomplished through advanced control), 1.3 refiner segment changes, 2. Power cost reduction by lowering mill peak power. The advanced quality control component was configured to minimize pulp quality variability while achieving the energy reduction objectives. The results from the project were very positive. Initially, there was a reduction in specific energy in main line refining in excess of 4% attributable to refiner segment changes. This was increased to a 7% reduction in specific energy when the advanced control was implemented on the mainline refiners. After final optimization of the mainline control system and implementation of advanced control on the screens and reject refiner the energy reduction was increased to more than 10%. Monthly peak power load at the mill was reduced from 80 MW to less than 75MW. This also resulted in a significant reduction in power costs. In addition to energy cost reduction, the project achieved the desired reduction in pulp quality variability. The freeness variance on mainline refiners was reduced by 31%. After reject and screen implementation, variance of reject refiner freeness was reduced 10% compared to the level it reached with only mainline control. The quality improvement was not limited to the TMP mill. A measurable increase in MD Tensile and CD Tear occurred on both paper machines during the same time period. Since completion of the project in November of 2005 the system has sustained energy cost savings for the Pine Falls mill.
机译:2004年底,Tembec Pine Falls工厂与美卓的造纸和自动化部门合作,通过始终如一地以最小的电力成本生产高质量的纸浆,实现了最佳的精炼性能。这些目标要求实施高级控制和实时优化技术,并结合主干精炼机上的精炼机分段配置更改,以证明这一概念并独立衡量分段和控件的节约贡献。由于已经实现并保持了显着的节能效果并大大降低了纸浆质量波动,工厂决定永久安装主线系统,并扩展了控制和优化措施,以结合筛分和废料精炼。还实施了轧机峰值功率控制和优化模块,以通过管理轧机总功率和峰值负载来优化运行。在该项目中,采用了四种降低能源成本的关键机制:1.通过以下方式降低特定的能源消耗:1.1自由目标转移(可能由于可变性降低),1.2精炼机运行的优化(通过高级控制实现),1.3精炼机段的更改,2通过降低工厂的峰值功率来降低电力成本。先进的质量控制组件配置为在达到节能目标的同时,最大程度地降低纸浆质量变化。该项目的结果是非常积极的。最初,由于炼油机细分市场的变化,主线炼油的单位能耗降低了4%以上。当在干线精炼机上实施高级控制时,单位能耗降低了7%。在对主线控制系统进行最终优化并在筛网和废品磨浆机上实施高级控制后,能耗降低了10%以上。工厂的每月峰值功率负荷从80兆瓦减少到小于75兆瓦。这也大大降低了电力成本。除了降低能源成本外,该项目还实现了所需的纸浆质量变异性降低。主干磨浆机的游离度差异降低了31%。在剔除和筛分实施之后,与仅通过主线控制达到的水平相比,剔除磨浆机的自由度差异降低了10%。质量改进不仅限于TMP轧机。在同一时间段内,两台造纸机的MD拉伸强度和CD撕裂强度均有可测量的提高。自2005年11月该项目完成以来,该系统一直为Pine Falls造纸厂节省了能源成本。

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