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FAILURE EVALUATION OF THE COMPRESSOR VANES OF A COMBINED CYCLE UNIT

机译:联合循环机组压缩机叶片的故障评估

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A compressor blade failure was experienced on a 69 MW gas turbine of a combined cycle (C.C.) unit after four years operation since its last overhaul (January 2005). The unit accumulated 27,000 service hours and 97 start-ups since the last overhaul. This unit consists of four gas turbine stages and 19 compressor stages and operates at 3600 rpm. In 2006, the unit was equipped with a fogging system at the compressor air inlet duct to increase unit power output during high ambient temperature days (hot days). These fog water nozzles were installed upstream of the compressor inlet air filter without any water filter/catcher before the water spray nozzles. Three unit failure events occurred within a small time period, which caused a forced outage. The first failure occurred in Decemberrn2008, a second event in March 2009 and the third event in Mayrn2009. Visual examination carried out after the first failure indicated that the compressor vanes (diaphragms) had cracks in their airfoil initiating at the blade tenons welded to the diaphragm outer shroud at stages 3, 8, 9, 10 and 11. Also, a number of stationary vanes and blades at each stage of the compressor showed foreign object damage (FOD) and fractures at the airfoil. Visual examination performed for the second failure event after 60 unit operating hours indicated that many compressor vanes (diaphragms) and blades had FOD at the airfoil. This was attributed to fractures caused by the fogging system. The water spray carried over in the compressor flow path at high velocity causing the FOD damage. Visual examination completed upon the third failure event after two unit startup attempts indicated damage of compressor stationary vanes and blades, principally at stages 12 to 16, and also stages 17 to 19. The damage consisted of airfoil fracture in the stationary vanes and blades, FOD, blade tip rubbing, and bending of the stationary vanes, blades and diaphragm shrouds.rnA laboratory evaluation of stationary vane tenon fracture indicated a high cycle fatigue (HCF) failure mechanism, and crack initiation was accelerated by corrosion pitting on blade surfaces due to high humidity air generated by the fogging system. Stationary vane damage was caused by a rotating stall phenomenon, which generates vibratory stress in stationary vanes and blades during unit start-ups. During the third failure event, the stationary vane HCF damage was highly accelerated due to pre-existing partial fractures in the tenons generated during previous failure events which had not been detected by non-destructive tests. Stationary vane and moving blade failure was also influenced by high tenon brittleness in stationary vanes and blades generated during manufacture by welding the diaphragms, and repair welding the blades without adequate post-weld heat treatment (stress relieving). A compressor stationary vane and blade failure evaluation was completed. This investigation included cracked blade metallographic analysis, unit operation parameter analysis, history-of-events analysis, and crack initiation and propagation analysis. This paper provides an overview of the compressor failure investigation, which led to the identification of the HCF failure mechanism generated by rotating stall during unit start-ups, highly accelerated corrosion generated by the fogging system, and high brittleness in the stationary vanes and blades as the primary contribution to the observed failure.
机译:自上次大修(2005年1月)运行四年后,联合循环(C.C.)单元的69 MW燃气轮机出现压缩机叶片故障。自上次大修以来,该部门累计服务了27,000小时,启动了97次。该单元由四个燃气轮机级和19个压缩机级组成,工作转速为3600 rpm。 2006年,该设备在压缩机进气管处配备了雾化系统,以在高温环境下(炎热天气)增加设备的功率输出。这些雾水喷嘴安装在压缩机进气过滤器的上游,在水喷嘴之前没有任何水过滤器/捕集器。在短时间内发生了三个单元故障事件,这导致了强制停机。第一次失败发生在2008年12月,第二次发生在2009年3月,第三次发生在2009年5月。首次故障后进行的目视检查表明,在第3、8、9、10和11阶段,压缩机叶片(膜片)的翼型出现裂纹,该裂纹始于焊接到隔膜外罩的叶片榫。压缩机每个阶段的叶片和叶片均显示异物损坏(FOD)和翼型断裂。在运行60个小时后,对第二次故障事件进行了目视检查,发现许多压缩机叶片(膜片)和叶片的机翼处都有FOD。这归因于起雾系统造成的断裂。喷水以高速流过压缩机的流路,造成FOD损坏。在两次单元启动尝试后,在第三次故障事件后完成的目视检查表明,压缩机固定叶片和叶片的损坏主要发生在阶段12至16,还有阶段17至19。损坏包括固定叶片和叶片的机翼断裂,FOD ,叶片尖端的摩擦以及固定叶片,叶片和隔膜护罩的弯曲。rn实验室对固定叶片榫的断裂进行了评估,结果显示出高循环疲劳(HCF)破坏机理,并且由于高应力而在叶片表面上产生腐蚀点,从而加速了裂纹的萌生。雾气系统产生的潮湿空气。固定叶片的损坏是由旋转失速现象引起的,该现象在机组启动时会在固定叶片和叶片中产生振动应力。在第三次故障事件期间,由于先前故障事件期间生成的榫舌中预先存在局部断裂,因此静叶片HCF损坏得到了极大的加速,而这种破坏还没有通过非破坏性测试进行检测。固定叶片和活动叶片的故障也受到固定叶片和叶片在制造过程中通过焊接隔膜产生的高榫眼脆性的影响,这些叶片在未经适当的焊后热处理(消除应力)的情况下进行修补焊接。压缩机固定叶片和叶片故障评估已完成。这项研究包括裂纹叶片金相分析,单元运行参数分析,事件历史分析以及裂纹萌生和扩展分析。本文概述了压缩机的故障研究,从而确定了在机组启动过程中旋转失速,雾化系统产生的高度加速腐蚀以及固定叶片和叶片的高脆性等产生的HCF故障机理。对观察到的故障的主要贡献。

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