首页> 外文会议>ASME(American Society of Mechanical Engineers) Power Conference; 20040330-20040401; Baltimore,MD; US >Resolution of Circulating Water Pump Problems Caused by Low River Levels at the Neal North Generating Station
【24h】

Resolution of Circulating Water Pump Problems Caused by Low River Levels at the Neal North Generating Station

机译:尼尔北部发电站因河水水位低而导致的循环水泵问题的解决

获取原文
获取原文并翻译 | 示例

摘要

Low winter water levels are causing reliability problems with once-through circulating water pump systems at several coal-fired power generating plants sited along the Missouri and Mississippi Rivers. River bottom degradation and potential COE river management changes make low river levels a likely on-going problem especially during drought years currently being experienced in the Midwest. This paper outlines circulating water pumping problems that have occurred at MidAmerican Energy's Neal North Energy Center due to low water levels in the Missouri River, and the steps taken to resolve these problems. Remedial design solutions that were either considered or implemented, such as supplemental pumps, vacuum lift systems, suction scoops, a new river water intake, and converting to a closed-loop cooling tower system, will be discussed. An in-depth discussion will be made on the supplemental pump system installed in the fall of 2002 and currently in operation on the Unit 3 river intake. Applicable permitting requirements will also be discussed. The new supplemental pump system consists of six submersible axial flow pumps mounted on the front of the existing Unit 3 intake. The total flow capacity of the six supplemental pumps is around 220,000 gpm which is discharged into the existing intake to maintain an acceptable wet well water level for the existing circulating water pump to operate. Other system components include an overhead monorail system to facilitate annual supplemental pump installation/removal, a floating ice deflector system, and a warm-water discharge splash plate. The supplemental pumps are installed and operated during winter months when river levels are low, and removed during the river navigation season when the COE maintains higher river flows.
机译:冬季低水位导致密苏里河和密西西比河沿岸的几座燃煤发电厂的直流循环水泵系统出现可靠性问题。河床退化和潜在的COE河管理变化使河水位低可能成为一个持续的问题,特别是在中西部目前正经历干旱的年份。本文概述了由于密苏里河水位低而在中美能源公司的尼尔北能源中心发生的循环水抽水问题,以及解决这些问题的步骤。将讨论已考虑或已实施的补救性设计解决方案,例如补充泵,真空提升系统,吸水铲,新的河水取水口,以及转换为闭环冷却塔系统。将对2002年秋季安装并目前在3号机组取水口运行的辅助泵系统进行深入讨论。还将讨论适用的许可要求。新的辅助泵系统由六个潜水式轴流泵组成,这些泵安装在现有3号机组进气口的前端。六个补充泵的总流量约为220,000 gpm,排入现有的进水口,以维持可接受的湿井水位,以使现有的循环水泵运行。其他系统组件包括高架单轨系统,以方便每年进行辅助泵的安装/拆卸,浮冰偏转器系统和温水排放溅水板。辅助泵在河流水位较低的冬季安装和运行,在COE保持较高河流流量的河流航行季节将其拆除。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号